By Jeff
Smith Photography: Jeff Smith Brought to you by Chevy
High Performance
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Where did the notion come from that adding more fuel to an
engine makes more horsepower? It’s one of those automotive
myths that clings to life even in the new millennium. It seems
just about every hot street car on the planet runs too rich
and could use a sharp tune-up. The latest victim in our quest
to rid the world of pig-rich hot rods was our pal Don
Swanson’s ’64 small-block El Camino.
A few months ago, CHP contributor Tim Moore put the tune-up
on Kevin Doyle’s mild 350-powered Camaro (“Attention to
Detail,” Dec. ’01). After we doubled the Camaro’s fuel mileage
while sharpening both the throttle response and tailpipe
emissions, it didn’t take long for his pal Don Swanson to ask
us to do the same with his car. Swanson’s El Camino presented
a much greater challenge since the small-block sported a lumpy
Isky 280/292 flat-tappet hydraulic cam that idled in neutral
with barely 8 inches of manifold vacuum. Compounding the
problem was a tight converter that pulled the engine down to
under 6 inches of vacuum in gear. The rest of the engine
included ported iron heads, headers, an Edelbrock Torker
single-plane intake manifold, and a modified Holley PN 80508
750-cfm vacuum-secondary carburetor.
Swanson complained that the small-block ran rich, fouled
plugs, and had a serious off-idle stumble that would sometimes
cause the engine to stumble under light acceleration from a
stop light. Swanson brought the El Camino over to Moore’s
shop, and we went to work. The first thing that Moore did was
check the idle emissions with his Sun HC/CO meter to establish
a baseline. The Sun machine tests four gases (HC, CO, CO2, and
O2) but we were most concerned with hydrocarbons (HC) and
carbon monoxide (CO). With the engine at operating
temperature, we measured a ridiculously rich HC idle of 1,500
parts per million (ppm) and a CO of 2.4 percent. CO percentage
can be used to indicate air/fuel ratio. The 2.4 percent figure
meant the engine was running at a reasonable 13.5:1 air/fuel
ratio. However, the HC level was especially high. Our goal was
to reduce the HC and CO to help the small-block run leaner and
crisper. We decided to shoot for reducing the HC down to
around 500-600 ppm, which would be a decent idle for a cam
this large.
First off, Moore noticed that Swanson’s motor was equipped
with suppression-type plug wires. While almost brand-new, the
wires measured 10,000 ohms of resistance. This is a little
high, so we replaced the suppression wires with a set of Crane
spiral-core FireWires that measured less than 500 ohms total.
Moore then fired the engine back up and checked the timing.
Using a new MSD self-powered timing light, the engine showed
14 degrees initial.
Moore also checked the idle mixture screws and found the
passenger-side screw was turned out only 1/8 turn while the
driver-side screw was over 1 turn out. Moore balanced the
idle-mixture screws at ½ turn each. If the idle-mixture screws
were turned out (richer) any more, the idle HC emissions went
dead rich. This indicated that the idle feed restrictors in
the carburetor were too large, allowing too little idle
mixture screw adjustment. |
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But before he could tackle that problem, we noticed that
after revving the engine a couple of times, the initial timing
was stuck at 34 degrees instead of the original 14. We pulled
the HEI distributor cap and discovered the small plastic
bushings that fit over the mechanical weight pivot pins had
failed, allowing the mechanical advance weights to stick.
Moore offered two new replacement bushings, and he cleaned and
lubricated the weights and reassembled the distributor.
With the timing stabilized, he could now address the rich
idle mixture. After pulling the carburetor and removing the
primary metering block, we discovered that the idle feed
restrictor for the carburetor had been drilled larger. The
standard idle feed restrictor size for most 750 cfm Holley
carburetors is around 0.034-0.035 inch. The restrictors in
this carb had been drilled to a larger 0.055 inch!
While this sounded bad, a typical big camshaft often
requires larger idle feed restrictors because the increased
overlap requires more fuel to keep the engine running. But we
also knew that the idle-mixture screws offered almost no
adjustment range. We used some 0.017-inch diameter electrical
wire strands and placed one inside each idle feed restrictor
in the metering block. This reduced the area of the
restrictor, which leaned the idle circuit.
We reinstalled the carb and allowed the motor to warm up.
Moore’s first step was to readjust the idle-mixture screws,
which now had a much greater range of adjustment than before.
However, a test drive revealed an off-idle hesitation that,
according to Swanson, had always been there but was now much
worse. He again removed the carburetor and discovered the next
common problem with big cams. Because of the long overlap and
reduced idle vacuum, the throttle blades had to be opened more
to allow enough air in for the engine to idle properly.
This larger throttle-blade opening uncovers a large portion
of the idle-transfer slot (see photo 9), which draws fuel from
the slot at idle. When the throttle is opened more, there is
insufficient fuel to compensate for the additional air
entering the engine. All of this occurs before the main
circuit tips in fuel from the boosters. The result is an
aggravating off-idle stumble. The cure required pulling off
the carburetor again.
We removed the baseplate from the carburetor and drilled
two 3/32-inch holes in the leading edge side of the primary
throttle blades. After cleaning all the metal chips from the
baseplate, we reinstalled the carburetor for another
testdrive. Drilling the holes allowed us to slightly close the
throttle blades, covering most of the idle transfer slot. A
quick test drive revealed that the off-idle stumble had
changed characteristics, but was still there! We were
frustrated. |
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By paying close attention to how the engine reacted, we
figured out what was happening. If Swanson eased the throttle
open, the carb worked fine. But if he hit part-throttle
quickly, the engine would hesitate and sometimes die
completely. This wasn’t a full-throttle stab, but more like a
1/8-throttle blip. After a few trips around the block, we
returned to the shop and discovered clearance between the
accelerator pump linkage and the pump arm at idle. This
allowed the throttle to move roughly 10 percent before the
accelerator pump squirted fuel into the primaries. The clue
was that Swanson’s engine would accelerate just fine when the
throttle was opened gently. We adjusted the accelerator-pump
arm to move in unison with the linkage and solved the problem.
Our next testdrive was much more rewarding—the engine
responded to throttle input crisply and without hesitation.
Swanson was thrilled.
Finally, we again plugged the El Camino into Moore’s HC/CO
machine and recorded the numbers. We didn’t gain a tremendous
reduction in HC/CO like we planned because the big cam just
wouldn’t allow the engine to idle with a leaner air/fuel
ratio. The best numbers we were able to achieve without
hurting driveability was a rather high 1,008 ppm HC and a CO
of 1.08 percent. What we did achieve was increased efficiency
in part-throttle operation and a crisper throttle that has
made Swanson’s El Camino a joy to drive. And that made all the
effort worthwhile. |
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Article Sidebar: |
The Sniff Test |
CO to Air/Fuel Ratio Chart |
Old Wives’ Tale |
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Article Source: |
Crane Cams |
Moore Automotive |
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Click
to enlarge photo |
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Click
to enlarge photo We started by pulling Swanson’s
immaculate ’64 El Camino into Moore’s shop and connecting the
HC/CO “sniffer” to read the exhaust emissions. This would give
us an accurate baseline. The carb is a Holley 750-cfm
vacuum-secondary piece with a Percy’s adjustable primary jet
plate installed. |
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Click
to enlarge photo First we replaced the existing
suppression spark plug wires with a set of Crane Firewire
8.5mm spark plug wires. The original suppression wires checked
between 8,000 and 10,000 ohms of resistance. The Crane wires
came in between 200 and 300 ohms. With lower resistance, more
spark energy is delivered to the plugs, which makes the engine
run more efficiently. |
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Click
to enlarge photo Next we tried turning the idle-
mixture screws but discovered an extremely small range of
adjustment. This indicated an overly large idle feed
restrictor so it was time to pull the carb apart.
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Click
to enlarge photo Before we repaired the carb, we also
checked the timing with MSD’s new self-powered timing light,
which has an extremely bright strobe that is very easy to see.
We found 14 degrees initial timing the first time, but after a
couple of revs, this jumped to over 34 degrees. Clearly there
was something wrong inside the distributor.
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Click
to enlarge photo We removed the cap and rotor and
discovered that the tiny plastic bushings that fit between the
mechanical-advance weights and the pins were wasted. Moore
replaced the bushings, and once the distributor was back
together, we reset the initial timing to 18 degrees with 36
degrees of total timing. |
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Click
to enlarge photo We found a piece of 0.017-inch
electrical wire and cut two short lengths that we placed in
the idle feed restrictor to reduce the overall area from 0.55
inch to 0.038 inch. We hoped this would lean out the idle
circuit and reduce the HC emissions. |
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Click
to enlarge photo The smaller idle feed restrictors
dropped the HC level, but a quick testdrive revealed a
now-worse off-idle stumble. We pulled the carb and found much
of the transfer slot uncovered. |
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Click
to enlarge photo A cam with a ton of overlap will
require a larger throttle-blade opening where a large portion
of the idle transfer slot (arrow) is uncovered. This creates
an overly rich idle mixture and an off-idle stumble.
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Click
to enlarge photo After testing with another carburetor,
we drilled the two primary throttle blades with a 3/32-inch
drill bit. This bleeds more air into the manifold, allowing us
to close the throttle blades so that only a small portion of
the idle transfer slot is uncovered (arrow 1). Arrow 2 points
to the curb idle discharge hole. |
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Click
to enlarge photo After resetting the idle mixture and
idle speed, the next test drive revealed improved throttle
response, but the engine still hesitated on light acceleration
off-idle. We readjusted the accelerator pump arm and the El
Camino instantly responded with its best throttle response to
date. |
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Click
to enlarge photo 1A clear indicator that the motor
suffers from massive overlap is the black carbon that has
coated the venturis of the carburetor. The carbon is the
exhaust soot reversion present in the intake manifold at low
engine speeds that contaminates the incoming charge. This is
why the engine requires so much fuel at idle.
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